15 July 2008

The Grind

A great but totally unenjoyable job done recently was to grind the interior of the hull, in preparation of adding bulkheads etc. Three of us worked solidly for about 3 hours, then I finished off over the weekend with about another 12 hours grinding. The dust was incredible, inches thick in the bilge and requiring hours of cleaning up. In preparation for grinding we removed the fiberglass layer over the top of the keel. This revealed a stinking black layer of ooze, made up up of who knows what.

Once the keel started to dry it started look look (and smell) a lot better.








As part of the grinding exercise I cut the backing off the chainplates, leaving a facing that we will tie into the boats structure a lot more effectively. As I did that I was horrified - but not particularly surprised - to find the wood filling in 3 out of 6 chainplates to be past salvaging. One was eaten by termites, the other 2 were wet and rotten. This one shows the termite residue, unfortunately not great detail.

This one shows a screwdriver hanging out of the bottom of the wood, after being pushed in very easily.

Up forward we have added a laminated plywood beam to carry the new Maxwell windlass, with a cross member to support the staysail stay. These are shown still covered with peel ply, which allows us to carry on glassing, painting etc, without sanding, once the peel ply has been removed.

The engine room bilge has had the fiberglass removed to let the underlying cement dry out. I think we need to come up with some ideas about a sump in this area.

26 June 2008

A Start at last

Well, it finally happened - Bill the boatbuilder turned up at my house and we began working on the boat! I had been helping him on another job for about a month, then we raced to Fiji together, which was great as we got to discuss the job a little. Anyway, one of the first jobs that Bill did was to cut a hole in the foredeck. This will be the hatch for the anchor locker, so the bulkhead on the aft end will be watertight. The locker will drain overboard and there will be an empty void under the floor.

One of the unpleasant things we have found (not totally unexpected) is significant rot under the deck. I think the main point of entry was under the forestay fitting, as back in Hawaii we found that the threaded rod connecting the forestay to the stemhead was broken. The fitting had lifted at some previous time and let the water in, rotting the plywood pad under the forestay as well as allowing water to wick back through the plywood core. The centreline appears to be OK, while it is quite rotten along the outboard edge. We have been cutting 73mm holes in various places and heating the inside of the boat in an attempt to dry the area out but I think we might have to be more aggressive with our treatment, maybe more holes and more heat.


The anchor locker bulkhead is all ready to fit and that will make me very happy - it is very exciting to be putting stuff in rather than taking it to the dump!



We can even say something is finished - Bill gelcoated the inside of the locker today and there is nothing else to do to those two surfaces. A small but very satisfying victory.

It has taken me quite some time to finish the cover over the boat, there has been some difficult engineering created to ensure we can park cars, access the garage etc etc, while trying very hard (well a little bit anyway) not to piss the neighbours off. We have had some pretty windy and wet days and it is still in place so fingers crossed it will stay there.

We have also removed the two forward hatches, which both collapsed as soon as the were lifted off the sealant. There is a raised fibreglass lip which is very lightly screwed on to the back of the teak base. We will need to cut these flanges off for the new Lewmar hatches.

20 March 2008

Hello Beta

It seems like a cargo cult at present, still waiting for the boatbuilder to finish on his current job and make a start here. To fill in the time I have been shopping, always a little dangerous. Anyway, my first major purchase has arrived, a very shiny new Beta BV3300 75hp engine. I'm impressed!

25 February 2008

Goodbye Mr Perkins

Well, finally got a friend to help direct the hiab and we removed the engine. It came out very easily, even with the gearbox still on. I have sold it to a friend who has a Peterson 44 with a dodgy motor.



Below the engine was a foetid mixture that would probably resemble the time long ago when life began. I have bailed out about 20 litres of stinking black stuff. I am looking forward to having this area cleaned out and newly painted.



The saloon floor came out with a little struggle and exposed the 2 "stainless steel" water tanks. It was hardly "stainless" and full of holes, someone had attempted to patch it with fiberglass. It was quite a job to pull these out of the walkway hatch by myself!



So, the next stage is to clean up a little!